Ian V
To answer your first question, no I didn't progress with the flash boiler for the picket boat. The coil was wound in a figure 8 configuration, and I made a twin poker type burner for it. For insulation, I carved something out of firebrick and surrounded the whole lot with a sheet steel casing. It all ended up surprisingly heavy. At this time, I was told about work done by someone on fitting a probe in his loco boiler in order to light up a couple of LEDs indicating high and low water levels so he could see what was happening when running at night. Now I'm not into electronics, but I did realise that if you could light a LED, you could do all sorts of things. Discussing this with Roy Verden (whom I believe you have been in contact with) He designed a system for operating a servo that would open and close a by-pass valve using a single sensor in the boiler. So the flash boiler was abandoned and replaced with a return flue one. Surprisingly, this weighed about the same as the flash setup.
Moving on, as you are only interested in running at relatively low pressure, the following may be of interest. Before building the picket boat, I had a model of the Victorian steam yacht "Greta". This was 44" long with a 5" beam and weighing around 15lbs. Over it's life it had about four different boilers and six different engines. One of the most successful combinations was with a flash boiler and V twin oscillator. But in addition to the flash coil, a steam drum was mounted above the coil. Unfortunately I've no photos. As far as I can remember, the coil was about 10ft of thin wall 1/8" stainless tube wound round a ¾" former giving a coil some five or six inches long. This was curved upwards at the outlet end, and fed into a copper drum one inch diameter and around four inches long. This drum was purely a steam reservoir and retained pressure well enough for the engine to be stopped for up to 30 seconds or so. It was fitted with a safety valve set at 30psi. The engine was a ½" bore and stroke V twin oscillator with feed pump driven at 1/3 engine speed. The large gear had a range of tapped holes in it so that the pump stroke could be altered. Firing was with a gas blowlamp. Propane rather than one of the butane mixes.
This all worked quite well. With any change in throttle setting, the amount of water pumped in obviously varied, the only downside was that the burner was always at the same setting. The coils got very hot with the engine stopped, but this did not seem to be a problem.
Hope this is of interest
Regards Malcolm