A while has passed since my last post on the conversion, this was due to a technical malfunction of the engine or to put it another way; i dropped it & bent the b*****y thing. Fortunately SteamboatPhil came to my rescue & its running sweetly again..
Everything is now installed in the boat & I have fired it up a couple of times to set up the automatic boiler control & sort out the teething troubles. A few leaks due to not wanting to overtighten anything & strip threads were easy to cure. Only the main Steam valve needed re soldering, which wasn't too bad.
The new ceramic burner proved a little troublesome, its body proved to be too close to the water gauge sensor & was going to overheat it if something wasn't done. I had the old blow lamp type burner from the boiler which was tried & found to be better. Although it doesn't put as much heat, so far it seems sufficient Maybe a bigger jet will help, but thats to be decided when the sailing trials start.
The gas control side of the ABC worked well, but the water gauge sensor didn't work. Don't know if its the sensor, the ABC box or the wiring causing troubles there, but it will all come out tomorrow & hopefully the problem can be sorted.
The water pump didn't circulate the water, but seemed to prime itself OK. One of the leaks was on the output from the pump & this speeded up with the engine, so it appears to be pumping. There is a way to suck the water up the water tank return pipe, which I will try next time.to see if it works once the whole system is full.
The servos were left disconnected for first few tests so as not to overcomplicate things.There seems to be some leaking of steam past the throttle control lever which, whilst not enough to run the engine, seems to be making the reversing lever much harder to move & I'm not sure a servo is up to this. The Gemini engine also revs much slower than the old electric motor, so a coarser prop may be required.
Considering the pump wasn't refilling the boiler, the plant still managed to run the engine for around 15 Min's before the water level fell too low. The engine wasn't under load & should use less steam when it is, as i was running it fast most of the time.The side tanks hold around another 2.5 boiler fulls of water, so I'm hopefull to get a reasonable sail time from the set up. The water/ oil trap was very effective, as not a single drop of water was expelled out of the funnel.It also transfered heat to the gas tank nicely, just keeping it slightly warm to the touch. & no pressure drop was apparent during the runs.
Not to many issues really for initial tests, only the ABC system worries me slightly as its not possible to replace a faulty control unit. The other problems are easier to fix, & this is the bit I enjoy about steam anyway.
its not just a bolt in & away you go type of propulsion, making it run well is the interesting part for me, & the satisfaction comes from achieving that.
Cheers Glenn